
Ford claims the short block is non servicable - it's not even mentioned in the Haynes manual - but that's never stopped us. We removed the big end caps and bearings, which was easy, followed by the main bearings, which was not. The bearing ladder is fun as you don't want to rock it and damage surfaces . We had to weld a socket to the end of an angled spanner in order to remove the bolts that go through the bearing seal - they're tucked behind the fly wheel under a lip and no spanner I had would reach them.

Number 1 cylinder bearings were melted, and the rest were starting to go, but fortunately the journals were ok. The main beaings looked pretty good but we decided to replace them at the same time. These can be removed by spinning them out one by one. We used a "spatula" made out of some thick plastic and wooden pushers made from dowl that had been filed flat at the edge to ensure nothing marked the surfaces. Once they started to move you could rotate the crankshaft and spin them out the rest of the way. Its best to replace each one as you go along or the crankshaft moves slighly on its axis, making replacement much more difficult. Don't ask how I know this......

We got replacement bearings from Raceline. They were very helpful in advising us - had it been a 2.3L engine we would've been in a lot of trouble as they are apparently much more sensitive to bearing size. They usually require the full monty of testing with plastigauge and multiple trial fits. Next we replaced the con rods with ARP items and then torqued everything back into place. The sump was refitted, the engine topped up with a full 5 litres of finest and the key turned. After a few tense turn overs the oil pressure shot up and we connected the ignition for a firing. It all went smoothly and now we have a knock free engine.

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